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dc.date.accessioned2022-04-06T15:13:34Z
dc.date.available2022-04-06T15:13:34Z
dc.date.created2022-03-01T19:11:27Z
dc.date.issued2021
dc.identifier.citationFagerlund, Johan Zevenhoven, Ron Thomassen, Jørgen Tednes, Marius Abdollahi, Farhang Thomas, Laurent Nielsen, Claus Jørgen Mikoviny, Tomas Wisthaler, Armin Zhu, Liang Biliyok, Chet Zhurkin, Andrey . Performance of an amine-based CO2 capture pilot plant at the Fortum Oslo Varme Waste to Energy plant in Oslo, Norway. International Journal of Greenhouse Gas Control. 2021, 106, 1-14
dc.identifier.urihttp://hdl.handle.net/10852/93369
dc.description.abstractFortum Oslo Varme AS (FOV) decided (in July 2018) to build a 1:350 scale pilot plant to demonstrate that the selected Shell’s CANSOLV capture technology using solvent DC-103 is suitable for cleaning CO₂ from the exhaust gases of their waste to energy (WtE) plant at Klemetsrud in Oslo, Norway. This paper presents the most important measurement data and results from a pilot plant testing campaign from March to December 2019. The project stated requirements for the successful completion of the first pilot plant campaign were at least 2000 operational hours and total amine emissions lower than 0.4 ppmv on average over the last 500 h of testing. Emphasis is on the online emission measurement results both with and without an aerosol emissions mitigation system located downstream of the capture unit. The impact of perturbations in the plant operating conditions and inlet gas quality is discussed, in particular the particulates content. The pilot plant campaign achieved its primary purpose of demonstrating low amine emissions. It also produced important data on absorbent degradation in actual operation on WtE flue gas while confirming other performance parameters such as CO2 capture efficiency, steam consumption and CO2 product purity. Thus, it can be concluded that the all requirements according to objectives of the pilot campaign were successfully met.
dc.languageEN
dc.rightsAttribution-NonCommercial-NoDerivatives 4.0 International
dc.rights.urihttps://creativecommons.org/licenses/by-nc-nd/4.0/
dc.titlePerformance of an amine-based CO2 capture pilot plant at the Fortum Oslo Varme Waste to Energy plant in Oslo, Norway
dc.typeJournal article
dc.creator.authorFagerlund, Johan
dc.creator.authorZevenhoven, Ron
dc.creator.authorThomassen, Jørgen
dc.creator.authorTednes, Marius
dc.creator.authorAbdollahi, Farhang
dc.creator.authorThomas, Laurent
dc.creator.authorNielsen, Claus Jørgen
dc.creator.authorMikoviny, Tomas
dc.creator.authorWisthaler, Armin
dc.creator.authorZhu, Liang
dc.creator.authorBiliyok, Chet
dc.creator.authorZhurkin, Andrey
cristin.unitcode185,15,12,0
cristin.unitnameKjemisk institutt
cristin.ispublishedtrue
cristin.fulltextoriginal
cristin.qualitycode1
dc.identifier.cristin2006815
dc.identifier.bibliographiccitationinfo:ofi/fmt:kev:mtx:ctx&ctx_ver=Z39.88-2004&rft_val_fmt=info:ofi/fmt:kev:mtx:journal&rft.jtitle=International Journal of Greenhouse Gas Control&rft.volume=106&rft.spage=1&rft.date=2021
dc.identifier.jtitleInternational Journal of Greenhouse Gas Control
dc.identifier.volume106
dc.identifier.doihttps://doi.org/10.1016/j.ijggc.2020.103242
dc.identifier.urnURN:NBN:no-95939
dc.type.documentTidsskriftartikkel
dc.type.peerreviewedPeer reviewed
dc.source.issn1750-5836
dc.identifier.fulltextFulltext https://www.duo.uio.no/bitstream/handle/10852/93369/1/1-s2.0-S1750583620306678-main-1.pdf
dc.type.versionPublishedVersion
cristin.articleid103242


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Attribution-NonCommercial-NoDerivatives 4.0 International
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